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93fox

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Everything posted by 93fox

  1. 93fox

    Newb

    Nice fox. I see your one that actually got their quicktime kit, glad to see it worked out. Welcome.
  2. 93fox

    Newb Here

    Sweet car, welcome.
  3. The fork should only go in one way. Ive had the best luck with an adjustable cable or stock cable and stock quadrant.
  4. Dont forget the mls gaskets and studs
  5. Thanks man, I drive it everywhere.
  6. Awesome, I thought it was you. Anyway, thanks again for the help and the hookup on the regulator.
  7. Yes sir, daily driven as much as possible on 10psi.
  8. Tremec with upgraded internals, 26spline input 31spline output, pretty much a tko600 with a centerforce dual friction.
  9. Yes, daily driven. Ramsey, never made it to the track.
  10. Yup, had to have the regulator, without that, it said it was running out of fuel at like 400, never ended up making it to the track
  11. Wanted to give a HUGE thanks to Brian at Dynotune while I was up in Ohio getting my car tuned and all the trouble he went through to help me out. You will not find a more stand up and helpful guy like Brian. Ill give you a rundown of how things went.... We strapped the car to the dyno friday afternoon, after doing some pulls and some tuning, we noticed the car was puking some coolant after each pull, couldnt really figure it out that day, so we said we will mess with it saturday. Got there saturday morning and we were able to confirm that the motor had a blown headgasket after doing several hours of picking our brains and doing several tests. Sunday rolls around, Brian was curteous enough to not only help me tear the car down and put it all back together, but he also allowed me to do all of this is his own shop because I really didnt have the space or time to do it back at my moms house. When we were tearing it apart, we noticed that where the headgasket had blown into the waterpassage, the dow pin that goes from the head to the block was unusually taller than all the other dow pins. We are still not for sure if thats what caused the gasket to go, but it just seems kinda fishy that that is where the gasket blew. Tuesday, we finish putting things together and it fired right up!! No problems what so ever, and it even sounded better/healthier, Brian obviously knows what he is doing. We decide to wait til wednesday to dyno it because he had a bike to do and he had really busted his ass putting the car back together. Wednesday suddenly appears, strap it to the dyno go to fire everything up and...............the computer that runs the dyno had suddenly crashed. Brian worked ALL DAY ( 12+ hours, till about 1130 that night) to back everything up on the computer and reload everything just to get it to read the dyno. Thursday, everything seems to be working and Brian gets to cranking on tuning the car. Keep in mind, this car has a mind of its own, ask anyone that visted the shop while I was up there. It would idle fine, rev fine, be under load fine, then just decide that it didnt want to work, AT ALL. Brian worked his magic and was able to get the car to run unbelivieably well. He was able to squeeze 488/516 out of a stock bottom ended, headed, and cammed motor!!!!! Once again, a HUGE thanks and praise goes to Brian for going above and waaaaaaaaay beyond for helping me out in a real time crunch. I know it wasnt the best as far as timing goes, but I owe Brian BIG time and probably will be for the rest of my life lol. I will be spreading the word down here in florida about Brian and someday hopefully bring him future business from people down here. Brian will be the ONLY tuner to touch or tune ANY of my cars in the future. If you want a stand up tuner that is not afraid to bend over backwords and go to great lengths to help you out, Brian at Dynotune is the right choice. Thanks again!! -Also wanted to say thanks to Mike(schmuck) for helping out during the whole process, it was greatly appreciated. Duff, for all the help he did with tearing it down and putting it all back together. Also, I think, Dkilbourne is his name on here, for the help and the fuel pressure regulator.
  12. Well...........? Updates.....???
  13. I wasnt able to ever pull codes with mine either, and it worked fine.
  14. 93fox

    dyno

    Dynotune motorsports hands down.
  15. Good looking notch man, good luck on the build.
  16. What you doing tonight? Track ya...??
  17. Thanks man, when you going to bring your car out? Might be going to CC&C tomorrow.
  18. Ya, lets see what it can break/ruin now lol. Nice meeting you and thanks for the info/help.
  19. Going to try to make this one while Im in town. Duff should be with me.
  20. Sounds good to me, just give Brian a call. I think he has a car to retune real quick in the afternoon and we should be leaving when he is done.
  21. I put a couple miles on it tonight, the street manners on this car are amazing. Im going to drive it around some more tomorrow, thinking about going up to marion tomorrow.
  22. Open downpipe, no exhaust on it yet.
  23. Where to begin with mine.....
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